First session with the ProSeal. I got everthing ready, rivet gun, back riveting set and plate, cut up shop paper towels and put them in a Pyrex bowl for pouring MEK over them. Soaked the rivets and cleaned the parts. I’m using the ProSeal tubes, so the mixing and application was very easy. I mixed it up a little early. I should have taped in all of the rivets first. I got into a pretty good rythm of frosting up a stiffener, pushing it down, back riveting, and then covering the shop heads with ProSeal. I have a fairly small back riveting plate. I ended up going off the end of it twice, but then didn’t do it again the whole rest of the session. Hopefully I’ve learned that lesson now. After riveting on the first stiffener, I noticed little dots on the skin. Doh! Forgot to wrap a rag around the rivet gun to keep it from spitting oil on the skin. Cleaned up with MEK and continued on.

I next attempted to back rivet the fuel flange. That did not go as well. The flange is curved, and I didn’t have it pushed down on the back riveting plate hard enough at the very front and back. The rivet heads were proud of the skin. Drilled them out (which is not fun with ProSeal everywhere) and tried them again pushing down on the flange this time. Worked much better. One rivet that I drilled out was stuck in the fuel vent line clip, so luckily I had a spare clip to use instead. Pulled off all of the tape and cleaned up with MEK.

I had planned to do the drain and coat some of the fuel sender parts, but 3 hours of messing around was enough for one day and I was getting hungry for dinner.
Dealing with the ProSeal and MEK was not too bad. But that’s what they all say after the initial session. I ended up using almost 1/2 of a tube. It was starting to set up pretty good after 1.5 hours, so I doubt I could have used the whole thing anyway.