The alternator air door flange set up well overnight. I’m using the “fast” hardener, and it’s still taking a while to set up. I moved the part inside to keep it warm, which I think helped. I drilled out the holes again that got filled up with epoxy and used a deburring tool to clean up the dimples.
Overnight I thought about how to attach the pop rivets. In other locations where pop rivets are used in fiberglass, they are backed up with a washer. In this location, you don’t want any chance of the washer getting loose and falling into the air intake of the engine. I hate to think of what a washer would do to the inside of the engine. I had some left over #4 washers I ordered a while back, which is the perfect size for 1/8″ pop rivets. I decided to use the washers, but epoxy them in place. I used some JB Weld under the washers, pulled the pop rivets, and then added a little more JB Weld over the top and around the edges. The washers aren’t going anywhere and the pop rivets won’t pull through the epoxy. (Sorry for the fuzzy pics.)

I then attached the door and gave it a try. Works excellent. This is something that will stay closed 99.9% of the time. The only time it gets opened is if the air filter gets clogged up for some reason.

After lunch, it warmed up enough to do a priming session. It’s been a long time since I’ve done any priming. I actually like it, because I know the next step is final assembly!
I was hoping this weekend to get the baffles to the point of trimming them to the cowl. I got pretty close. I feel anyway that I’m over the major hump with these crazy baffles. I spent a ton of time going part by part, doing any last trimming and drilling. A few things have to wait until after the baffles are trimmed to the cowls, like the oil cooler.
This appears to be a common problem. With everything screwed down, this one flange just wasn’t sitting right. Cranking it down would have tweaked everything around it to the point of not fitting.

I ended up cutting off the flange and using a short chunk of .063 x 3/4 x 3/4 angle. I also made the stiffener for the back right side wall from the same angle stock.
I bent the back bulkhead bracket some more. It was about 3/8″ short of where it needed to be. I then drilled the back bulkheads to it.
I also drilled the two back left bulkheads to each other and did some final filing around the engine.
I have a bunch of riveting to do now, but the baffles are basically ready for trimming to the cowl after a lot of hours on them this weekend. Yeah!!