Finally worked up the nerve to test the left fuel tank again. I hooked up the manometer with fairly high hopes. It lost 1/2″ after an hour. Not good, but maybe the temp just went down. It lost another 1/2″ after that and then another. Not good.
I pulled the tank outside, put a ballon on one of the fittings and pumped it up. I sprayed soapy water all over the tank and couldn’t find anything. On the third time around the tank, I finally noticed a few small bubbles on one of the fuel filler flange rivets. (You can just see it in the second picture below.) It’s the one that is holding the fuel vent clip. I had trouble with that rivet when I installed it. I didn’t tip the tank on the back rivet plate to account for the bend in the flange and the head ended up proud of the surface. I had to drill it out and redo it. Well, I must not have had enough ProSeal in that one the second time around.

Rather than mix up a whole batch of ProSeal for one rivet, I’m going to fix it when I work on the next tank. Hopefully I can just reach through the fuel filler hole and dab some ProSeal on the inside of the rivet.
Anyway, I’m moving on. I’m quite certain that the baffle is no longer a problem. Woo hoo!
I put the fuel tank on the wing. Things were not lining up well. I had gunked up the ProSeal on the baffle flange a bit thick. I cut that down a bit. Still not fitting. Then I remembered someone on the list saying they had a similar problem that they solved by jacking up the middle of the wing a bit more. So I pumped the jack once–better. Twice–perfect fit. Eventhough I used a line across the spar to make sure it was lined up, I guess there was still a millimeter or two of sag.

A side note on fuel tank testing. I left the ballon on the tank just for fun. After several hours, there was no noticeable decrease in size, eventhough I know I have a small leak. I’d suggest using the manometer method instead of relying solely on a balloon for testing the tanks.